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First, thanks to Eric for all the videos. They’ve helped immensely the last few years.
Ok, I’ll start with details on the model and symptoms, then what all I’ve done and results from testing.
I consider myself an above average capability DIY’er. That I haven’t been able to fix it yet is really frustrating. So I turn to the ETCG hive mind.
North American 1999 Kia Sportage EX
4×4
K08A model/spec
As far as I can tell, completely stock, no mods. Bought used a couple months ago to be used as a road legal hunting, fishing, beach, light trail rig, and it has never run right for me.Currently, the main symptoms:
-Intermittent rough shaking idle at ~650 rpm, but doesn’t stall.
-Surging while slowly getting up to speed. The worst is accelerating between 30 and 65 mph, either almost no power at 2000 rpm or surging at 3000+ rpm. Once up to 70+ mph it settled at about 3000 rpm and was fine so long as it didn’t need to downshift.
-No power. Very slow acceleration, and would lose speed quickly trying to go up any kind of hill when cruising at highway speeds.
-Intermittent no or very little throttle response when starting from stop.
-It all gets worse when the engine heats up and heat soaks everything.
-Occasional stall when giving gas from stop. This happens when the engine is cold and is a newer symptom.
-Running very rich. Smell of fuel when the engine struggles and already shiny black fouling on the new plugs (only ~600 miles on the plugs). Varying long term fuel trim of -5 to -17.
-Early on it threw the pending codes P0171: System too Lean (Bank 1), P0301/302/303/304: Cylinder 1/2/3/4 Misfire Detected, P0300: Random/Multiple Cylinder Misfire Detected. Haven’t seen these codes since I started messing with it.
-After screwing with it for a couple weeks, I also saw pending P0604: Internal Control Module Random Access Memory (RAM) Error, P0101: Mass or Volume Air Flow Circuit Range/Performance Problem.
-Most recently trying to get out to the highway for a hunting trip, it threw up P0123: Throttle/Pedal Position Sensor/Switch A Circuit High Input
-Currently no codes stored in ECM.
-One of the 30A fuses in the engine bay box wasn’t blown, but looked like it had arced and melted the plastic. See pics in gallery.
-Electrical gremlins?
-Guy I bought it from insists it ran fine until he power washed the engine bay to make it look nice for sale.What I’ve done:
Many pictures of the work I’ve done so far, and some screen shots of Torque live data. http://imgur.com/a/pZxTI
-Replaced the entire ignition system. Everything. Pigtail/ignition wire harness–>Coils with boots–>Plug wires–>Plugs
-Verified proper resistance values of plug wires and coil boots.
-Replaced PCV
-Cleaned MAF with electric parts spray. Hosed out IAC with carb cleaner.
-Took vacum line off of FPR for 5 minutes. No gas leaking out.
-Replaced fuel filter.
-Connector to ECT sensor seems good.
-Cleaned and scuffed to shiny the ground points on manifold, battery tray, access plate to fuel pump, and under driver and passenger kick plates. The main ground for ECM is under the passenger kick plate. See pics in gallery.
-Recall for infamous C123 and C124 connector problems was done in 2000.
-Checked for vacuum leaks with the carb spray method. Nothing. Took the nipple off the intake mani to induce a vacuum leak to see what it would sound like and how the live data reacted. As far as I can tell, and what Torque live data is telling me (consistent -20ish at idle), there is no vacuum leak.
-Replaced TPS because of some inconsistent/spiking TPS readings at idle and while driving that seemed to coincide with the surging.
-Checked TPS with multimeter. Bad ground? https://youtu.be/PGra7zhX8U0
-Found high resistance values in various places. For example 3 ohm from negative post on battery to just a few inches away on the main clamp/connector. Difficult to get meter to read ground in expected places around the engine bay.
-Graphed live data from O2 sensors. Both do the switching voltage thing at idle, and then constant higher voltage at 2k rpm. http://imgur.com/mIZYETM
-Did dry compression test and got 120psi on all four cylinders, but….the engine was cold, I didn’t disable the fuel, and I wasn’t holding the throttle wide open. Will repeat with fuel disabled and throttle wide open, but can’t warm up engine with everything taken off.So that’s where I’m at.
I’m at a loss of how to start addressing the electrical issues. I already cleaned all the ground points. The only other thing I can think of is to replace the clamp connector on the negative battery post.
My other guesses are:
-Cracked exhaust mani, and/or problems with the O2 sensors and warm up cat. Having trouble getting to the sensors. Going to have to cut away some of the heat shield.
-Static/mechanical timing is off, either from the belt slipping a tooth or two, or the woodruff key and keyway are messed up because someone didn’t toque the bolt on the crank nose correctly.Thanks all.
Cheers!
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