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2003 Blazer; 4.3, 4L60-E; 97,000 miles; 2wd

Home Forums Stay Dirty Lounge Service and Repair Questions Answered Here 2003 Blazer; 4.3, 4L60-E; 97,000 miles; 2wd

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  • #567497
    AnthonyAnthony
    Participant

      Little back story here. I bought this blazer a few months back. I believe in August. I never noticed the problem at first, but what happens is above 3000 rpm’s the engine just bounces off the tachometer without shifting(it’s quite scary actually, always feel like it’s going to over rev.) I was getting an intermittent P0355 for the CPS. So I started doing research. I replaced the TPS with a slight improvement now it would be able to get to about 3500 rpms, then it would jump. But now it would start to actually shift (albeit a firm “hard” shift.) I thought I heard it pinging when it jumps up(or the timing chains or valves, I can’t tell) so I replaced the fuel filter, cleaned the air filter (K&N it was filthy) and I pulled the CPS on the harmonic ballancer to check for contact. There were no visible signs of contact, so I cleaned it off, and re-installed. Then I performed a CPK variation re-learn procedure. After that the car would drive a lot better. I can hit about 4,000rpms, then it would do the same thing. Sometimes it would shift, and sometimes it wouldn’t. I immediately got a full tank of fuel after this procedure, and after driving home, literally about 5 minutes after I did the CPK relearn, the Check engine light came on again. This time entirely new. I got a P0300, and (2) P0304’s. Random misfires, and cylinder 4 misfires. Also, a hard start condition developed. No matter the temperature of the car. So I performed a tune up. I replaced the cap and rotor(both terribly corroded) and I replaced the wires and spark plugs. All the plugs I pulled were clean with no signs of oil burning. They smelt good too. After that I cleared the code and took the car home. On the way home the CEL flashed again, but then went out. I assumed it was miss fire again. I read the code and got a P0101, for the MAF. I did remove it to gain access to the driver side spark plugs. So naturally, I cleaned the MAF, and cleared the code. It has not yet returned. The hard starting seems to be getting better but I haven’t driven it enough to really know for sure yet. But, now when I drive the car, I can hit 4-4500 RPMs and I still get the same problem. My first ever WOT with this car was yesterday, and I didn’t hold it long enough to see if it would shift, I thought the engine was gonna go. To shed some light, once it hits the certain RPM range it feels as if the trans is in neutral, and never tries to shift. Normal driving is just fine, anything below 4k and it drives perfect. I currently have no check engine lights. I do believe there may be a knock, I can never really tell. I am trying all the cheap alternatives, I can not afford to take it to a shop. I am in the military, and make barely any money.

      So, to wrap up. I have received codes P0355, P0300, P0304, and P0101. I have replaced the TPS, fuel filter, cleaned the air filter, cleaned the MAF, replaced the cap, rotor, wires and plugs. I did a CPK relearn. The hard start only occurred after the CPK re-learn. The problem is getting steadily better… But still, the car does not run as it was intended. No I don’t drive it WOT every where, but I need the full power band to pass, and what not. Any help would be appreciated.

      Random bits of info.

      There are slightly larger tires on the truck than stock, and my speedometer is 3mph slow. I just changed the oil with 5w30 Valvoline Synpower, and a mobile one oil filter. When I bought the car it was 1.5 gallons low on coolant. Don’t know how long it was low before that. It doesn’t over heat, and hasn’t been leaking since then. No moisture on the oil cap, and the coolant looks good. There is no smoke coming from the exhaust. Everything works as it should. The car drives perfect until I get into it. The fan clutch may be going out.

      here is a video from before I did any work. I will get a new video of the current state asap
      http://s204.photobucket.com/user/pwnthis/media/Blazervid_zps3706ab28.mp4.html

      Edit: There was no build up on the screen on the top of the distributor. Apparently Ionic gas vapors (something the guy at the Auto Hobby Shop we have on base told me about) build up on this screen. Well mine was clean, and clear.

    Viewing 15 replies - 46 through 60 (of 72 total)
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    • #571666
      AnthonyAnthony
      Participant

        So I got my blazer back today. Nothing has changed. The mechanic said he replaced the plug for the CKP sensor, and he replaced the fuel pump relay. But the car is exactly the same. He also said the misfire is only at 2500 rpms. Other than that, nothing.

        #571667
        Kevin CriswellKevin Criswell
        Participant

          Did he check the timing chain slack?

          I like to pull the sensor and look inside at the sprocket with a light. Something is vibrating at 2,500 rpm and causing that misfire.

          Ask him if he has an labscope. You really need that signal wire scoped at 2,500 RPM and see if the signal goes bad.

          #572371
          AnthonyAnthony
          Participant

            Does anyone have any experience with this? I read somewhere that a sticking exhuast valve, or I suppose intake valve could do the same thing. I did the paper trick (holding it up to the tail pipe and watching to see if it shakes back and forth) and it wasn’t. I don’t want to take it to the dealer. And I am sick of working on it. What do y’all think? Ignition, fuel, or air? Could it be the PVC?

            #572855
            AnthonyAnthony
            Participant

              Well something interesting to report. I replaced my CKP sensor for the hell of it. Well my tachometer no longer acts funky, however I still get a misfire at 2450 rpms exactly. ANd I have that hard start still..

              #572961
              AnthonyAnthony
              Participant

                So I bypassed the fuel pump relay and had the pump on constantly. No change! Truck took forever to start. I threw so,ex carb cleaner in the intake and it didn’t start any faster. Checked for vac leaks…none.

                On a separate not I mistakingly fixed my windshield wipers.

                #573397
                AnthonyAnthony
                Participant

                  Well, I have discovered something today. I started my car, and I could smell so much un-burnt fuel. So I got to thinking, maybe there is a fuel leak in the spider, and its flooded which is why it wouldn’t start. Probably why it wouldn’t start with the starting fluid either. So, I put the car in flood stop, (flooring it while cranking) and it still started. The only reason I am not sure about this theory, because it runs fine! AND the Diagnostic computer shows that the car isn’t running rich or lean. So maybe the fuel pressure regulator is leaking when there is no vacuum??? I am going to pull this intake off this week and take a look.

                  #573675
                  AnthonyAnthony
                  Participant

                    So I redid a fuel pressure/leak down test. Fuel pressure was 58psi with engine off, and 56 psi at idle. Once I turned the engine off, and after about 3-4 minutes the pressure dropped to 35 psi and still dropping. I need to pull the plenum off and check out the injector for leaks…

                    #573680
                    Steven CummingsSteven Cummings
                    Participant

                      Not sure on the type of fuel pump; on my moms Chrysler 300M, it had excellent fuel pressure, but would quickly lose the pressure when off. The leak was a bad return on the pump, nothing in the engine side. But like you said, you smell fuel as well; I didn’t.

                      #573684
                      Kevin CriswellKevin Criswell
                      Participant

                        [quote=”tonyroc14″ post=84477]So I redid a fuel pressure/leak down test. Fuel pressure was 58psi with engine off, and 56 psi at idle. Once I turned the engine off, and after about 3-4 minutes the pressure dropped to 35 psi and still dropping. I need to pull the plenum off and check out the injector for leaks…[/quote]

                        If you take the 3 bolts out of the throttle body on the intake you can see into the plenum with a light and see if the lines are leaking.

                        #573689
                        AnthonyAnthony
                        Participant

                          [quote=”Raistian77″ post=84480][quote=”tonyroc14″ post=84477]So I redid a fuel pressure/leak down test. Fuel pressure was 58psi with engine off, and 56 psi at idle. Once I turned the engine off, and after about 3-4 minutes the pressure dropped to 35 psi and still dropping. I need to pull the plenum off and check out the injector for leaks…[/quote]

                          If you take the 3 bolts out of the throttle body on the intake you can see into the plenum with a light and see if the lines are leaking.[/quote]

                          Thank you. I’ll do this tomorrow

                          #574359
                          AnthonyAnthony
                          Participant

                            I haven’t had time to look because my wife has been in town, but I am getting 13mpg now as opposed to the 17mpg I was getting.

                            #575746
                            AnthonyAnthony
                            Participant

                              Well, I ordered my parts. Fuel injector, and gasket.

                              #575949
                              EricTheCarGuy 1EricTheCarGuy
                              Keymaster

                                Good luck. Keep us posted on your progress.

                                #576301
                                AnthonyAnthony
                                Participant

                                  Well I replace everything today. The fuel pressure regulator was leaking. Stars right up now! However a new check engine light came on..I’m eating right now but on my way home I’m going to check it out

                                  #576345
                                  AnthonyAnthony
                                  Participant

                                    P0304. Same old code. It’s funny because I can never feel it.

                                  Viewing 15 replies - 46 through 60 (of 72 total)
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